duminică, 26 decembrie 2010
Beyond Foam
miercuri, 1 decembrie 2010
Scenery Tests
duminică, 14 noiembrie 2010
Switch installed on SR
The last photo shows the installed switch and most of the wires connected. Up next is testing that the motor can be unscrewed from this position (I didn't drill another hole through the foam+wood board since there are already quite a few) and connecting this switch to the existing SR track that's already glued.
duminică, 31 octombrie 2010
PT segment track status: complete
Finally the track on the PT (pre-tunnel) segment it's glued and electrically interconnected. It took quite some time because of the many little things that had to be done/fixed:
-various feeders had to be extended, since the original size was too short and they couldn't reach the space underneath the switch motors, were they're supposed to connect
- a couple of sections of track already cut to size had to be readjusted, because the original dimensioning wasn't done with one end firmly connected to the next piece of track, but rather simultaneously on both sides, hence small errors; but just an extra 1 mm in flex track length becomes a large problem since the track starts to buckle
- holes were drilled through the plywood for the PT switch pair
- the holders for the switches/switch motors on the PT segment had to be further tweaked, since the original versions were built just to get them up and running, but they couldn't properly sustain a train going over; so for the 3 switches on PT, a new plywood piece was glued next to the existing one holding the motor in place, and then different strip(s) of plywood were glued on the surface securing everything to the big foam board; for the first switch in the pair a foam holder was glued underneath the ballast piece since it was a better approach
- extra care was needed to avoid any kinks in the track pieces connecting to the switches, so pins and more pins and pins without the head were used
- for the second switch in the PT pair, the end of the remaining point blade also had to be extended since it wasn't staying in the tie plate, and with everything glued it gets pretty complicated to further modify the switch (the other point blade was extended here: http://piko-modellbahnen.blogspot.com/2010/08/test-driving-through-pt.html); the same old method was used, with 3 stranded wires soldered together forming the "extension", and this soldered to the tip of the point blade (originally i tried to solder on the outside of the blade, but the switch wouldn't go all the way through, so i used a small file to clean the solder and redo the same thing on the other side of the blade)
- a strange issue persisted with the (same) second switch in the PT pair - all the length of the switch is placed on a constant ramp, but the last portion (right over the switch motor) was level, which looked peculiar; all the various foam pieces - unglued yet -were measured and found to be the correct size, the switch itself wasn't bent and anyway it is rather flexible vertically, even in its foam ballast, so the only explanation could be that the big foam board was thinner in that exact spot; the fix was to use a strip of 1mm beneath all the supporting structures in this area as to "bump" the height
- the movement of the point blades on the first switch in the pair wasn't right in one direction; it seemed like the point blades would stall for a moment in one direction of movement; a little filling on a tie support causing this fixed it
- all 3 motors on the PT were unmounted, then remounted to test the access through the plywood holes; first the screw holding the actuating wire is loosened using a small enough ratchet that fits in the underneath hole, the actuating wire is removed from the mechanism, the 2 screws securing the motor to its plywood base are unscrewed and the motor then comes off; when remounting the screw for the actuating wire needs to be tightened a bit, otherwise the ratchet will not work, and the motor will have to be removed again to access this screw.
All the testing this weekend was done using the PIKO BR 01.5, since the Lenz BR 66 developed a small problem with one of its small rear wheels - namely a 'tick' every one revolution. I couldn't figure out exactly what causes it, so I mailed Lenz the exact problem, and they're sending a new type of wheels. Hopefully in about 2 days they'll arrive. As for the PIKO loco, I've spent quite some time with the desk lamp studying if the flanges touch the tie plates of the Tillig code 83 track, and couldn't come to a definite decision. However, after this weekend operating sessions, comparing the tie plates to their original state, several bumps on the plates seem to be a little shiny, a sign that sometimes the flanges do make contact. I'm looking into buying replacement wheels for the tender, since 2 of the motor wheels are located here and also because the difference in pulling power on the new Tillig track vs the old thick PIKO track profile is dramatic - the loco barely pulls itself on the new track. And it's definitely not because of any oily debris on the traction tires, since these were cleaned properly.
The photos: 1. final preparations before glueing the switches in place; 2. glueing the track under (proper) weights
marți, 19 octombrie 2010
LR track in place
duminică, 10 octombrie 2010
LR continued
- build the plywood that will support the motor and drill holes for the screws (2); drill a hole for the rod that will move the points
- drill a hole through the ballast (the one corresponding to the switch model - without the specific model the switch doesn't stay right !) in 3 places - corresponding to the feeders on internal/external point blade and one that sets the polarity on the frog
- cut the right path in the ballast for the rod that will move the points
- with switch mounted in its corresponding ballast piece and the motor attached to the plywood piece right under the switch - with the switch in one of the two positions (not anywhere between) - the postion of the ballast on the plywood is marked
- the spots on the track where feeders will be soldered must be cleaned properly - using a bistoury to remove any oxide, using different patterns of movement - not just left-right, because this will not remove all the oxide; then the feeders are soldered
Last week holes in the big wooden board were made for the switch on the bottom of the LR segment, and for the switch on PT right next to the tunnel. Also the switch on the top of LR was finally glued to position, and so was the one on the bottom of LR. The LR ramp has been completely glued (the red books are keeping everything together in this operation on the first photo). All the electrical connections were also done for the mentioned switches. Part of the line that makes the LR was glued to position, along with superelevated ballast: the difference in height is 1 mm, which is prototipically correct (on real railroads the height of the outer rail above the inner rail , also named cant, can have values of 100mm).
But the real shocker was the Gras Master + Silflor (or miniNatur, as they are sold in Europe). The result is just superb, and the 130 euros payed just for the GrasMaster are certainly worth it.
duminică, 3 octombrie 2010
Up, up, and away !
miercuri, 25 august 2010
Fixing track on SR
Right now about 3 weeks of vacation lie ahead, so the Paasche VL 1007 airbrush got a thourough cleaning, and the layout will get a rest. Last 2 photos show the Lenz BR 66 and the double decker car testing the now glued segment of track.
luni, 23 august 2010
Test driving through PT !
miercuri, 18 august 2010
duminică, 15 august 2010
PT switches painted
duminică, 8 august 2010
Pre-Tunnel Segment - one step closer
Next on the list was a minimal wiring - connecting all the return conductors (red on the 86112 Tillig switch motor), and the other 2 wires (pink/yellow) to a Phidget 1017 board. The return conductors were all connected to the center casette (a future post will detail the wiring), using a Viessmann connector (if you're looking for something like this - the code for the yellow one is 6842), while the Phidget and its corresponding wires were placed in a new casette that was dug, right below the front track in the second photo. Also new holes were carved in the foam board for easier access to the wires.
marți, 3 august 2010
Status Report 2
luni, 26 iulie 2010
Status Report 1
duminică, 30 mai 2010
Wiring
And since there was some spare time, I also started working towards installing an entry signal right next to the east tunnel portal. The signal will be a 4012 Viessmann - fitted with 3 lights - red, yellow, green. 4 wires have to be set-up for this one. Installing the wires is a bit complicated on this layout, because it wasn't build on just a plain wooden board. Back when it was designed, since there wasn't much space available in this room (it still isn't), the board was installed on 2 hinges, and it sits between 2 closets. When it's not in use, the layout is raised vertically, and a nice shiny wooden board appears. When it's being used, the board comes down.
Since wires couldn't just go through the board on the other side, a checkered maze of foam squares, about 1 cm high, was installed, and on top of this a foam board, about 3.5 cm thick. The plan was to route all the wiring through this maze. Unfortunately in practice it gets difficult, partly because the maze tunnels are getting crowded quickly by lots of wires, and adding new wires requires special equipment. So I started drilling access holes in the top foam board, for better access. In the second photo the wires are installed and labeled, ready for the new signal.
luni, 24 mai 2010
New Orders
Track Solutions
The new Lenz loco, just as the cleaning car, work just fine on this type of track, however most of the old PIKO rolling stock, because of the larger dimensions of the wheel flanges used back then, tends to lightly brush the ties as they go along. I could see 2 methods for fixing this - buy new wheel sets for the cars, and for the locos, where available, or use a grinder to reduce the diameter of the flanges. No solution was chosen at the time (actually I haven't made a decision to this day) but I studied further the track produced by Tillig, and found that they produced different models of curved switches, something I could only dream of with the PIKO straight switches I had. The decision was finally made that all track had to be changed.
Fixing Old Locos
DCC Testing
After encountering the same lack of electrical connection described in an older post, the decision was made to solder all the track pieces together, using thin wires, just as was done on the actual layout. The problems with the interference of the sparks and the optical detectors dissapeared, as no false readings were ever encountered.
Lenz also manufactures a computer interface, that connects to the USB port, so the problem of computer-controlling the layout seems solved.
Bottom line: DCC was the way to go, and cost of the decoders for the remaining locos was small compared to the value that the system brings.
More Investments
I also looked on the figures required for getting in DCC. I decided to go for Lenz, a german manufacturer. A few things are required to begin operating in DCC - a control station, an AC transformer, and compatible locomotives. The Lenz control station (LZV 100) and its remote control were 240 EUR. I didn't need a new transfomer at this stage, since I had the Viessmann one already, and for testing it should have been ok. Trouble was with the locos, since none of them were equipped for DCC. Converting old DC locomotives to DCC operation is done with a special decoder, that is installed inside the locomotive. One Lenz decoder was about 25 EUR, not a steep price, but i wanted to see DCC in action at its full potential, and this would just have been impossible with an old loco fitted with a decoder. So I looked around for a loco that was DCC compatible, and was cheap enough. TRIX made some locos at 70 EUR, and they had inside dedicated space, and a connector for the decoder. So the loco would cost just under 100 EUR, which was fair enough. But further browsing on the Lenz website revealed that they also produced 2 HO locos - a small diesel one, and a steam loco - BR 66, that would be perfect on the layout, since it wasn't too small, nor too long. The BR 66 came in at 180 EUR, and I decided to go for it. At the time I was also trying to fix a broken front headlight piece of the PIKO BR 01.5 steam loco - precisely a light guidance plastic part, that was previously broken and then glued, the result being that 2 headlights were ok, but the third one was dimmed. Also a small spring for the loco-tender coupler was damaged, and some wheels on the tender were quite rusted. Since PIKO had on its website dedicated pictures and codes for the replacement parts, I emailed them for further assistance. Unfortunately I got no reply, as I would later found out the support only works in german, and google translate will prove a success in communicating with PIKO. So I turned to LokShop, where I got the other orders so far, and they were happy to help. So in mid-february I made the order for the Lenz LZV100, the Lenz BR 66 loco, and the spare parts - a total cost of 450 EUR, with the spare parts less than 10 EUR.